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Sailings cancelled due to technical issues
Due to a technical issue on board, the 'Arrow' was sidelined, and as of Aug 2, the ferry 'Loch Seaforth' was operating the overnight freight service until further notice. As a result of this, the departure from Stornoway on Aug 2 at 9 p.m. and from Ullapool on Aug 3 at 12.30 a.m. were cancelled. All booked customers on cancelled or affected sailings were accommodated on alternative sailings. Repairs were completed on Aug 3.
Serious oil leak after net got entangled in propeller
The 'Arrow' which was chartered to provide extra sailings on the Stornoway service had to be taken out of service after completing just five return sailings on July 24, 2021, due to a serious oil leak in the propulsion system following a fishing rope entanglement around a propeller. The ship left Stornoway on July 25 at 7.15 p.m. with an ETA at Belfast for drydocking on July 27. The damage was to be inspected and repaired, and the sailings were cancelled until further notice. The ferry 'Loch Seaforth' has returned to carry out the overnight freight service. Repairs were exptected to take about a week.
Report: Crew was not fully prepared for pilotage in restricted visibility
The crew of the 'Arrow' which ran aground while entering Aberdeen Harbour in thick fog on the morning of June 25, 2020, was not fully prepared for pilotage in restricted visibility, an investigation of the Marine Accident Investigation Branch (MAIB) has found. An over-correction to get back on course was not noticed by the bridge team in time to avoid the grounding. Significant damage to the port side of the underwater hull was caused by the incident, which happened after an overnight passage from Lerwick. During its port approach, a pilot exemption certificate (PEC) holder provided by the vessel’s charterer was navigating by radar and steering the vessel. The vessel encountered the thick fog a few minutes before it entered Aberdeen’s 70-metre-wide navigation channel. The PEC holder became overloaded… with limited support from the bridge team. While attempting to correct a deviation to the north of the planned track, he over-corrected to the south – and that was not noticed by the bridge team in time to avoid the grounding. As a result of the actions taken following this investigation no recommendations have been taken.
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